Small update.
Larger tires improved spool a bit. I ditched the 1.5” drop springs and reinstalled OEM springs. Got my ride height up and swapped the 25.3” tall tires for some 27” tires. The car drives so much nicer on these horrible Kansas roads now. Unfortunately body roll is pretty bad. No more high speed off-ramp fun for me! I’m seeing full boost (25psi) by 4500-4600rpm now. Shifting at speed I never drop below this point so I think I’ll be good to go in the ¼ mile. Improved my MPG as well with the lower cruise rpm.
The OBX manifold cracked at the WG tube. I repaired and braced it. I’ll throw pics up later. The car looks pretty silly at this ride height!
Crack...



So here is my attempt at TIG welding. Swept wide to try for more strength.
Grabbed some scrap from the bin and made a brace as well. I'm picking up one of the 02 housing bolts for the brace. When I cleaned up the scrap I realized it was some type of old ruler! LOL I'll clean it up and paint it all later, I was pressed for time. The Flex WG exhaust is also a temp. fix. Although having the flex piping clamped to the down pipe also provides support. I didn't run any type of WG exhaust during the clutch break in period.

original and best looking of course.

Before


After

